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55 Posts
Drove my RC today and noticed it really lacked part-throttle power and required a lot of downshifting to 2nd to accelerate from 35 to 50.
Some background: truck was pretty much parked in late August 02 when I got my new Ram. Filled the tank with fresh gas about 6 months later. Drove the truck for a week around August 03, parked it again with partial tank of gas. Replaced the distributor, cap, rotor, and plugs a couple months ago at which time I ran 1/3 can of SeaFoam thru the TB and poured the other 2/3 in the tank that had about 1/4 full of gas (34 gal tank). Noticed truck still missing/backfiring, lots of loud ticking from injectors and poor spray cone.
This afternoon I replaced both injectors and the inline fuel filter. I drained the line from the filter to the TB. Drove it and put $10 of fresh gas in it to thin down the SeaFoam a bit (was just under 6 gal...geez).
Truck seemed slow taking off from a stop, requiring me to nearly floor it to accelerate at a rate on par with traffic. When I did floor it from a stop it seemed to take at least 10-12 seconds 0-60 and just three years ago I know it was less than 9 seconds 0-60.
Only once while I was out today did it backfire, and I had been doing 30, floored it causing a downshift to 2nd <backfire> then resumed accelerating.
Any thoughts on what might be causing this? IIRC, after I replaced the distributor I set the timing about 12 BTDC. I read the post about the stuck EGR and wondered if that might be contributing. Another thing, I removed the belt from my AIR pump years ago and never removed or plugged any of the other parts of the system, just slipped the belt off. Any thoughts would be appreciated.
Some background: truck was pretty much parked in late August 02 when I got my new Ram. Filled the tank with fresh gas about 6 months later. Drove the truck for a week around August 03, parked it again with partial tank of gas. Replaced the distributor, cap, rotor, and plugs a couple months ago at which time I ran 1/3 can of SeaFoam thru the TB and poured the other 2/3 in the tank that had about 1/4 full of gas (34 gal tank). Noticed truck still missing/backfiring, lots of loud ticking from injectors and poor spray cone.
This afternoon I replaced both injectors and the inline fuel filter. I drained the line from the filter to the TB. Drove it and put $10 of fresh gas in it to thin down the SeaFoam a bit (was just under 6 gal...geez).
Truck seemed slow taking off from a stop, requiring me to nearly floor it to accelerate at a rate on par with traffic. When I did floor it from a stop it seemed to take at least 10-12 seconds 0-60 and just three years ago I know it was less than 9 seconds 0-60.
Only once while I was out today did it backfire, and I had been doing 30, floored it causing a downshift to 2nd <backfire> then resumed accelerating.
Any thoughts on what might be causing this? IIRC, after I replaced the distributor I set the timing about 12 BTDC. I read the post about the stuck EGR and wondered if that might be contributing. Another thing, I removed the belt from my AIR pump years ago and never removed or plugged any of the other parts of the system, just slipped the belt off. Any thoughts would be appreciated.